On April 13, 2025, our cutting-edge 6-3/4”Hydro Thruster for oil based drilling fluid was deployed to the XX19-Q9-H3 well, at the request of a CNPC drilling company.
Performance Metrics
Drilling Footage: 3,295 meters in a single run
In-Well Time: 357.5 hours
Circulation Time: 307.5 hours
This showcases the tool's exceptional efficiency and reliability in challenging drilling conditions, contributing to significant operational success.
Key highlights of the operation:
Record-Breaking Footage: Achieved a single-run drilling footage of 3,295 meters, setting a new benchmark for efficiency (from 922 meters to 4,217 meters depth).
Extended Operational Durability: Operated for 15 days (April 15–30, 2025) with 357.5 hours in-well and 307.5 hours of circulation time, showcasing robust reliability.
Superior Performance: Effectively mitigated weight stacking challenges encountered in the build-up and horizontal sections, significantly enhancing drilling speed(ROP) and operational efficiency.
Stable and Powerful Output: Delivered consistent power and reliable performance, meeting all expected goals under demanding conditions.
Critical Technical Support: Provided essential support for the smooth and efficient drilling of the XX19-Q9-H3 well, reinforcing its value to CNPC's operations.
This innovative tool tackled weight stacking challenges in the build-up and horizontal sections, boosting drilling speed and efficiency. It set a new record for single-run footage and provided critical support for the well's success.
This milestone underscores our leadership in drilling technology and our commitment to delivering reliable, high-performance solutions for complex wells sections. Stay tuned as we continue to push the boundaries of oil and gas innovation!